Discovery II Talk about the Land Rover Discovery II within.
Sponsored by:
Sponsored by:

What did you do with your DII today?

Thread Tools
 
Search this Thread
 
Old May 31, 2017 | 03:04 PM
  #4051  
CollieRover's Avatar
Joined: Mar 2014
Posts: 2,620
Likes: 313
From: Chicago
Default

I am visiting my parents, have a garage so bedlinered my fender flares, ladder, and wipers. replaced Power steering pump and flushed the system. Sanded and clearcoated my headlights a la chrisfix on youtube.

Went well, got some overspray on my car as some newspaper became undone, but he flares and everything look much better. Not that anyone but myself will notice.
 
Reply
Old Jun 1, 2017 | 09:28 AM
  #4052  
zoltan7's Avatar
Mudding
Joined: Dec 2016
Posts: 197
Likes: 23
Default

no idea how you changed that pump and it isn't groaning. I'm battling mine hard currently
 
Reply
Old Jun 2, 2017 | 01:41 PM
  #4053  
CollieRover's Avatar
Joined: Mar 2014
Posts: 2,620
Likes: 313
From: Chicago
Default

Originally Posted by zoltan7
no idea how you changed that pump and it isn't groaning. I'm battling mine hard currently
This is the second time I have done it. Are you sure it is the pump that is groaning. TBH, my steering has been getting worse and worse, and I think it has been my steering box the whole time.
 
Reply
Old Jun 2, 2017 | 02:21 PM
  #4054  
zoltan7's Avatar
Mudding
Joined: Dec 2016
Posts: 197
Likes: 23
Default

I think it's the pump. I'm going to rebuild my old pump and try a few things on this new one to get her to smooth out. I think maybe just a tiny bit of air in the system somewhere (or a stiff seal)
 
Reply
Old Jun 2, 2017 | 02:49 PM
  #4055  
JUKE179r's Avatar
Camel Trophy
Joined: May 2016
Posts: 3,969
Likes: 859
From: Britainistan, UK
Default

I had a blown rear crankshaft seal which I honestly think was due to excessive pressure from adding a second FRAM PCV valve to the left side (drivers side) of the Bosch 4.0 engine. So a second $4 FRAM PCV valve cost me $750 plus down time driving Myrtle.
Possibly because of this additional PCV and additional bac pressure, my engine rear crank shaft seal is pissing out oil. Luckily the maintenance shop owner asked me what else I needed done since he would be working on it for a day. So he ended up replacing my modded front driveshaft and bolts/nuts (I've been procrastiniating installing it for months now), changed oil and filter, changed transmission filter/seal and fluid and installed new ignition coils for $750.

I bought a oil catch can from eBay and going to install it this weekend. Expect more pictures from my adventure....
 

Last edited by JUKE179r; Jun 4, 2017 at 11:29 AM.
Reply
Old Jun 3, 2017 | 10:26 PM
  #4056  
MacRoadie's Avatar
Mudding
Joined: Jan 2017
Posts: 141
Likes: 14
Default

Changed tranny fluid and filter, and transfer case oil. Transfer case is a PITA. Fill plug is blocked by parking brake cable and you can't get a straight shot at it due to brake drum.

Anyway, pretty sure the t-case had never been drained based on that plug location, the fact that it was in there pretty tight, and bone dry when it came out. Also just a guess, but I'd wager no more than a quart or so came out, but over 2 went back in.
 
Reply
Old Jun 4, 2017 | 01:56 AM
  #4057  
MrValingo's Avatar
Rock Crawling
Joined: Mar 2015
Posts: 284
Likes: 53
From: Madison, wi
Default

P0455. Gas cap wasn't on all the way....was it really that easy??
 
Reply
Old Jun 4, 2017 | 06:32 PM
  #4058  
CollieRover's Avatar
Joined: Mar 2014
Posts: 2,620
Likes: 313
From: Chicago
Default

Originally Posted by zoltan7
I think it's the pump. I'm going to rebuild my old pump and try a few things on this new one to get her to smooth out. I think maybe just a tiny bit of air in the system somewhere (or a stiff seal)
I have had mixed results rebuilding stuff, but I did rebuild my ABS Pump and that has worked out incredibly well.

I got my pump from Napa, and it had a limited lifetime warranty so they replaced it. Loved that.

My steering has been stiffish, and odd for years. I think the Steering box has been going, and blowing the pumps. I have one on order and am hoping that fixes for a while anyway.
 
Reply
Old Jun 5, 2017 | 12:56 AM
  #4059  
MrValingo's Avatar
Rock Crawling
Joined: Mar 2015
Posts: 284
Likes: 53
From: Madison, wi
Default

Clock is now led backlit. Bypassed the shuttle valve wiring. Cleaned the in-dash cup holder that's been sticking since I got the truck.
 
Reply
Old Jun 5, 2017 | 05:02 AM
  #4060  
zoltan7's Avatar
Mudding
Joined: Dec 2016
Posts: 197
Likes: 23
Default

Managed to successfully plated the rear frame and welded the broken bracket of my rear panhard bar back on to the frame.

Somehow must've arc'ed electricity or had a bad ground point lol because I fried both stainless extended lines in the rear I guess I can only hope I didn't smoke the ABS lines as well.

Woe is me lol
 
Reply



All times are GMT -5. The time now is 01:57 PM.